A series of MnCeOx catalysts supported on cordierite honeycomb (Cord) were prepared by a combustion synthesis method using Mn(NO3)2 , Ce(NO3 )2·6H2O and citric acid. The effect of the molar ratio of Mn/Ce, calcination time, the amount of citric acid and the effect of water vapor on the catalytic properties for the complete oxidation of benzene were investigated. These catalysts were characterized by X-ray diffraction (XRD), H 2 temperature-programmed reduction (H2 -TPR), O2 temperature programmed desorption (O2 -TPD) and scanning electron microscopy (SEM) techniques. The results indicated that the MnCeOx /Cord catalyst with Mn/Ce molar ratio of 1:1, calcining for 7h and M n+ /(citric acid) molar ratio of 6 exhibited the highest catalytic activity. When the concentration of benzene was 1500 ppm and the gaseous hourly space velocity was 20000h -1 , the conversion of toluene was 99.1% at the reaction temperature of 300 oC.
Larger amounts of alkalis, alkali earth metals and sulfides in flue gas from glass furnace were easier to deactivate selective catalytic reduction (SCR) catalyst compared to the flue gases from other stationary sources. Catalyst regeneration has been an emerging research topic for flue gas denitrification in glass furnace. Regeneration of the deactivated TiO2-ZrO2-CeO2 /Al2TiO 5 -TiO2-SiO2 (ATS) complex phase ceramics catalysts used for NH3 -SCR of NO x in glass furnace was studied in this work. Effects of regeneration methods, including washing with different aqueous solutions and sulfuric acid, thermal regeneration, thermal reduction regeneration, and thermal regeneration with SO2 , on catalytic performance were comparatively investigated. In comparison of catalytic activities between the catalysts before and after regeneration, results showed that washing was the most effective regeneration method, and the sulfuric acid concentration of the washing solution was an important factor. Washing time directly affected catalyst regeneration efficiency and catalyst life. The regenerated TiO2-ZrO2 -CeO2 /ATS catalyst regained more than 90% NO conversion after being washed with 10 wt.% H2SO4 for 30 min.